5.7 motor problems
#11
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Location: portsmouth rhode island
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Today I had some time to look at the motor again. I re checked compression in some of the cylinders #6 stayed the same at around 150 the others were even higher than before in the 240 range so I stopped testing. I think I mentioned before that I put marvel mystery oIL in each cylinder so I'm guessing that's causing the high numbers although I cranked the engine over several times before testing. I also did a leak down test on all cylinders here is what I found. #1 19% leaking through exhaust and rings #2 15% rings #3 30% rings/exhaust #4 18% rings/exhaust #5 25% oil/exhaust #6 55% exhaust #7 22% exhaust/rings #8 25% rings/exhaust. Im guessing with these results the heads need to be replaced?
#13
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So a little update. I tore the engine apart and brought the heads to machine shop just waiting for an update and repair. I have everything cleaned and prepped to go back together but I'm a little unsure on the assembly. basically I'm looking for the torque#s and sequence of the heads and intake, adjusting the valves and possibly retiming the engine.
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I'm not sure why the compression was so high the first time. the second time I had put mystery oil in each cylinder so that gave me a false reading. The heads were repaired I will be picking them up today. I was told that they were pretty bad but not sure what they repaired. I just hope this solves the reversion problem I've been having.
#16
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Im thinking you would have to pour mystery oil down the neck of your compression testor while your doing your test to achieve 240 on a contemporary marine engine. If reversion cooked your exhaust valves , and those boys slapped some low shelf valves in now , your not out of the woods yet