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What can make 500 EFI shoot oil out the dipstick tube?

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What can make 500 EFI shoot oil out the dipstick tube?

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Old 04-10-2017, 08:23 PM
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GNJ
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Default What can make 500 EFI shoot oil out the dipstick tube?

Refreshed both motors over the winter - top ends done on both motors.
Mobil 15-50w oil
Mobil 1 oil filters
Port engine oil pressure gauge reading 60psi at idle, starboard reading 40psi at idle. Launched boat and ran at 3300-3500 rpm for about 5-10 mins. Powered up to 4500 - 4700 rpm and then smelled oil. Gauge on port motor was pegged at 80psi! Other motor normal at 50psi. Stopped, open hatch, saw about 4 ounces of oil had spewed out of diptick tube all over front of engine.

The only thing I can think of right now is changing the oil filter bypass valve in the block (GM 25161284) I ruined the old one taking it out.

Anybody have any thoughts?
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Old 04-10-2017, 08:29 PM
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Sounds like you have some crank pressure coming from somewhere in the motor that's cause it to puke.
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Old 04-10-2017, 08:29 PM
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It is not an oil pressure problem, It is a crankcase pressure problem. Might just be because the rings aren't seated yet. Possible broken ring or the crankcase not properly vented.
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Old 04-10-2017, 08:48 PM
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compression checked?
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Old 04-10-2017, 08:50 PM
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or maybe detonation bad enough to damage the ring lands.
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Old 04-11-2017, 05:28 AM
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Bad injector melted a piston already? Usually something like that when you have severe blowby
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Old 04-11-2017, 06:40 AM
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Originally Posted by GNJ
Refreshed both motors over the winter - top ends done on both motors.
Just to make sure on the same page, last fall you indicated you only had 80hrs on the motors. Why the rebuilds again ? IE: What happened ?

For those who didn't see or remember this (like me) here is a thread he posted last fall with driveability issues and what performance parts are in these motors:
http://www.offshoreonly.com/forums/g...0efi-help.html
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Old 04-11-2017, 07:01 AM
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Originally Posted by SB
Just to make sure on the same page, last fall you indicated you only had 80hrs on the motors. Why the rebuilds again ? IE: What happened ?

For those who didn't see or remember this (like me) here is a thread he posted last fall with driveability issues and what performance parts are in these motors:
http://www.offshoreonly.com/forums/g...0efi-help.html
SB - Headers leaked and heads had to be refreshed.
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Old 04-11-2017, 07:05 AM
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Jeff32 - 120-125 on all 8. Leak down all around 10%
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Old 04-11-2017, 07:08 AM
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Is that cold? Sounds a little low for 500's
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