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Leak down test results
So I did a leak down and this is what found.
With a 100 psi going in, this is what I got #1-93psi #2-91psi #3-35psi intake valve leak #4-65psi intake valve leak #5-92psi #6-85psi leaking into #4 #7-30psi leaking into crankcase #8-93psi Added a little oil to #7 and it's up t 92psi. Pulled the heads and definitely was leakage between #6 and #4 at the head gasket. All I have on the history of this engine is it was build in 98'. Just before I got it there was some t-stat work done. But there wasn't one in it.. It's already .030 over with SP L2465 pistons. Still hone marks in the bores. I'm already thinking a bigger boat in the next year or 3 so don't want to dump a ton into this one. What would you do? Hone, rings, bearings, gaskets, lap the valves and run it is my thought.. |
Take it to a machine shop and have them tell you. Most likely you will need a valve job bore/hone . It never ends even trying to do it cheap
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How long has it been since last ride? Might consider a valve job and new gaskets and hope for the best. But #7 could have a broken ring so I'd pull the pan and that one at the very least. Won't take long.
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I've only got the boat wet once as I just bought it end of season. It ran decent for the one ride on a 38° day.
Don't know how long it sat before that. So there's#7 I'm thinking it was overheated.. That # 3 cylinder intake valve is warped. Did a quick lapping and there's one area not making contact. No evidence of it hitting anywhere. Cylinders have some rust stained areas and a few scratches I can feel. On the happy side, crank looks pretty good and hasn't been turned yet.. oh and one lifter was tight coming out. Can feel a burr on the bottom OD. So.... Let's build a new engine.. Going to finish tearing it down and drop it at the shop Monday. |
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Glad I took it apart..
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You might as well start tearing it down. Sucks but...
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Already done, and ready to go.
Better now than in July.. |
Originally Posted by convincor
(Post 4612197)
I've only got the boat wet once as I just bought it end of season. It ran decent for the one ride on a 38° day.
Don't know how long it sat before that. So there's#7 I'm thinking it was overheated.. That # 3 cylinder intake valve is warped. Did a quick lapping and there's one area not making contact. No evidence of it hitting anywhere. |
I was referring to the warped valve, and the head gasket failure.
as for #7, IDK. There's no marks in the bores in that area. More than likely caused by excessive heat and/or detonation. |
is this efi or carbed
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