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in my opinion it ran rich/carb flooded gas diluted the oil and killed it, does not talk much fuel in oil make it useless, did it one and could not believe how quick killed one...
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Machining the piston bores by hand with scotch brite and no piston clearance mite not be a good idea afterall. Never take your motor to a crack house to get built.
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Originally Posted by bck
(Post 4363899)
I might start a pro systems thread next so you can see that junk. It won't be nearly as long though, carbs are much smaller. Sometimes you just need to vent when you're writing checks you shouldn't have to for thousands of dollars
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Originally Posted by JMPH
(Post 4364173)
I curios , the pro systems carb was to blame, amongst you other problems?
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I see a couple Pistons that show signs of detonation. But as far as your main issue I'm with EZ on this one. Looks like oil contamination. If this is this case though the oil that came out of the motor should reek of gas. If you put your hands in it it should come right off and the inside of that motor should clean up very easily.
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Negative on the gas smell. Oil had just been changed, had maybe an hour or 2 on it. In my opinion Pro Systems carb not at fault, just an overpriced, overrated mediocre carb that wasn't close out of the box and needed to be rebuilt with worthless customer service in my opinion. Boat had afr meters on it, was still being dialed in. Engines less than 10 hrs total run time including dyno. *12 qt pans as well, lots of oil
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Originally Posted by Black Baja
(Post 4364190)
I see a couple Pistons that show signs of detonation. But as far as your main issue I'm with EZ on this one. Looks like oil contamination. If this is this case though the oil that came out of the motor should reek of gas. If you put your hands in it it should come right off and the inside of that motor should clean up very easily.
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What's the chances you gas washed the cylinders during tuning? I have seen it before on a carbureted engine killed the cylinders from the choke staying on.
Where any of the second rings stuck? Or it was lack of clearance piston to wall its in bad shape. Now I see its carbureted from pictures. |
My quick fuels were nearly spot on out of the box according to my widebands
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I'm considering the possibility that heat might have been the main cause at the moment. There are obviously issues that the builder is responsible for like the poor rocker geometry and mismatched pushrods, but ultimately the failure may be on me. What if overheating caused the out of round bore issues ? Possible? What if the bores were honed with torque plates and then were measured after disassembly without torque plates ? could that cause the bore issues?
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