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engine guys,,,build 468 won't run out

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Old 08-26-2019, 08:45 PM
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Originally Posted by Baja Rooster

As mentioned a plugged carb will give you a higher pressure reading than a functioning carb.

How do you figure that? My fuel pressure is the same 9 PSI at idle or WOT. A regulator is used to maintain a pressure.
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Old 09-18-2019, 08:04 PM
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Well, I thought I found it, secondary accelerator pump not fully pressed at wot. Still had a a big squirt left. Adjusted the nut, went back out, same thing, 4000 rpm at 3/4 throttle, no grain at full. Called dui dist. got a guy that knew nothing and had to go ask someone each question. They said " doesn't sound like a dist. problem." Gee, thanks DUI. Next will regap the plugs, although starting to think maybe a carb problem. Holley marine 850 double pumper. Carb worked fine on last engine. Only difference on the carb is I removed the choke.

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Old 09-18-2019, 10:29 PM
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did you check float levels both front&rear?
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Old 09-19-2019, 06:39 AM
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Only a suggestion, with boating season almost over... maybe pull engine and run on dyno?
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Old 09-19-2019, 09:24 AM
  #25  
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Originally Posted by daleroger
Well, I thought I found it, secondary accelerator pump not fully pressed at wot. .
Accelerator pump shot has zero to do with engine hp/performance. All it does is quirt fuel in when the airflow change is faster than the carb;s resultant added fuel flow. This keeps engine from lean pop backfire when accelerating.

You probably fuk'd the accelerator pump spec's. You are supposed to have some arm movement left when at WOT as you don't want to bottom it out. Search net for Holley Accelerator Pump Lever Adjustment so you put it back to stock.
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Old 09-19-2019, 09:52 AM
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So you changed heads cam compression exhaust and ignition and reused carb. Did you tune the carb to the new motor on a dyno,? Checked afrs? Plug chops at various rpms and loads ? I keyed in when you said the arb worked great on old motor, this motor is a completely different anima
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Old 09-19-2019, 10:16 AM
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Originally Posted by daleroger
Well, I thought I found it, secondary accelerator pump not fully pressed at wot. Still had a a big squirt left. Adjusted the nut, went back out, same thing, 4000 rpm at 3/4 throttle, no grain at full. Called dui dist. got a guy that knew nothing and had to go ask someone each question. They said " doesn't sound like a dist. problem." Gee, thanks DUI. Next will regap the plugs, although starting to think maybe a carb problem. Holley marine 850 double pumper. Carb worked fine on last engine. Only difference on the carb is I removed the choke.
Did you remove the choke blade completely or just disconnect the linkage? They have been known to "fly" closed if the linkage was disconnected and blade still installed.
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Old 09-19-2019, 10:42 AM
  #28  
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And if you are going to remove the choke blade you might as well go all the way and mill the choke tower off. Then tune.
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Old 09-22-2019, 12:17 PM
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yes, checked and set them both
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Old 09-22-2019, 12:19 PM
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it had a spring at the end of travel, so it doesn't bottom out, but you could be right about I made ot out of spec.
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