Slight milkshake on dipstick
#1
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Joined: Apr 2004
Posts: 217
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From: Charlotte, NC
Been running this setup for 5 years now. 540 ci NA motor.. aprox 9.1 comp. Roller motor..Timing locked out @ 34. Digital 6plus MSD box, MSD crank trigger and billet distributor. CMI Etop headers.
Cam: 114 Lobe Separation
Intake: 234 duration 572 peak valve lift @.050
Exhaust: 232 Duration 572 peak valve lift #.050
Crossover with merc pressure dump out the side. Block pressure never goes above 20psi. Hardine marine thermostatic oil filer head. Oil gets up to 220* in about 5-7 minutes from leaving the dock and never moves..
Made some minor adjustments this winter.
Changes
O2 Sensor bungs installed
Pyrometer bungs installed
1.6 ration intake rockers. (Exhaust same 1.5 ratio for past 5 years)
Outdrive gearing changed to 1.5 from 1.25.
Water lines from back 2 intake manifold ports to front 2 ports
Enlarged crossover to thermostat housing bypass line
Moved timing from 34 to 36.. Exhaust gas temps seemed to lower a bit with this change.
Motor was winterized the same way this year as all years past. Block fully drained. All water hoses including exhaust removed. Cooler water lines both removed. Antifreeze poured straight into block and into oil cooler. Motor was compression tested and leakdown tested last Oct (as done every year at the end). Still great numbers. Just about the same from year to year.
Got about 9 hours on the motor this spring so far. Running great. Checked oil level today and noticed some milkshake on the dipstick.. Nothing serious. But never ever ever there before.
Best guess I have right now is with the gear ratio on the outdrive changed the idle was able to be set lower.. close to 600 rpms in gear. Could this be reversion? I have not pulled any plugs yet.. Only other guess is the bungs in the exhaust were not sealed properly? (just a guess).
Any ideas?
One more thing. I check oil level almost everytime out.. This is the 5th or 6th run this spring and I have not noticed it before.
Cam: 114 Lobe Separation
Intake: 234 duration 572 peak valve lift @.050
Exhaust: 232 Duration 572 peak valve lift #.050
Crossover with merc pressure dump out the side. Block pressure never goes above 20psi. Hardine marine thermostatic oil filer head. Oil gets up to 220* in about 5-7 minutes from leaving the dock and never moves..
Made some minor adjustments this winter.
Changes
O2 Sensor bungs installed
Pyrometer bungs installed
1.6 ration intake rockers. (Exhaust same 1.5 ratio for past 5 years)
Outdrive gearing changed to 1.5 from 1.25.
Water lines from back 2 intake manifold ports to front 2 ports
Enlarged crossover to thermostat housing bypass line
Moved timing from 34 to 36.. Exhaust gas temps seemed to lower a bit with this change.
Motor was winterized the same way this year as all years past. Block fully drained. All water hoses including exhaust removed. Cooler water lines both removed. Antifreeze poured straight into block and into oil cooler. Motor was compression tested and leakdown tested last Oct (as done every year at the end). Still great numbers. Just about the same from year to year.
Got about 9 hours on the motor this spring so far. Running great. Checked oil level today and noticed some milkshake on the dipstick.. Nothing serious. But never ever ever there before.
Best guess I have right now is with the gear ratio on the outdrive changed the idle was able to be set lower.. close to 600 rpms in gear. Could this be reversion? I have not pulled any plugs yet.. Only other guess is the bungs in the exhaust were not sealed properly? (just a guess).
Any ideas?
One more thing. I check oil level almost everytime out.. This is the 5th or 6th run this spring and I have not noticed it before.
Last edited by JohnSchiavarelli; 04-11-2010 at 09:03 PM.
#4
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From: Charlotte, NC
I never removed the intake.. just took out the rear plugs and ran 6an line from rear to front..
#5
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From: Charlotte, NC
#6
Its most likely reversion or you have an internal issue. (Head gasket is my first guess) I would change the oil and raise the idle up to whatever rpm you turned with the old ratio. If the oil comes back reversion is less likely.
#7
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From: Charlotte, NC
The oil level has not raised. And there is NO milk what-so-ever in the upper half (valve area). the milk on the dipstick is light.. I mean very light..
#8
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Joined: Jul 2004
Posts: 11,332
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From: chicago
Im thinking the bungs might not have been welded up correctly. Your cam isnt to radical, plus i would think with the cmi headers reversion shouldnt be an issue. But just for he heck of it, i'd bump the idle up a bit to 700-750 in gear and see if that helps.
9 out 10 times, when a problem suddenly occurs, its most likely something you recently changed or messed with.
9 out 10 times, when a problem suddenly occurs, its most likely something you recently changed or messed with.
#10
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Joined: Apr 2004
Posts: 217
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From: Charlotte, NC
Im thinking the bungs might not have been welded up correctly. Your cam isnt to radical, plus i would think with the cmi headers reversion shouldnt be an issue. But just for he heck of it, i'd bump the idle up a bit to 700-750 in gear and see if that helps.
9 out 10 times, when a problem suddenly occurs, its most likely something you recently changed or messed with.
9 out 10 times, when a problem suddenly occurs, its most likely something you recently changed or messed with.



