Engine Guru's - Need help-Take a look
#41
I thought some might want to know what caused detonation of these pistons. In the interest of full disclosure I humbly present the facts, hoping it may help someone else someday.
I finished tearing down motor last night and this is what I found.
I noticed a rusty stain next to a freeze plug, and thought it a good time to replace while accessible. I popped the plug and immediately found my problem. Sand.... and a lot of it. And yes, directly under the piston that had the meltdown. In fact the entire side of block was loaded with sand. The # 4 cylinder was almost buried in it. there was no circulation happening on that side of motor. If you recall, my #8 cylinder was showing sign of detonation as well. Apparently I must have done some good clammin with the outdrive the week before, during the night. I never knew how much sand i actually sucked in. Running in river up here, you sometimes get a lot closer to the bottom than you would like. I never ran it hard until the following week, when damage became apparent.
As for symptoms or lack of :
-Still had good water pressure ( yes I will still replace pump)
-Never showed hot on gage. Sending unit is next to thermostat and was still getting cold water flow
-The only thing I noticed was right side valve cover was getting hotter than other side.
So there it is in a nutshell. My bad..
I am still looking to get back in water with reasonable budget. I need pistons, heads, and will also replace valvetrain. I am trying to track down a set of 781's locally. If anyone has some hardware for sale, I will listen. Would like to stay with ovals. I would also appreciate some ideas regarding cam/piston/compression combo's that's been proven to work well. Thinking about staying with hydraulic flat tappet for budget reasons.I may upgrade rockers though. I have performer intake with 750 carb and EMI's to bolt up.
Thanks guys
Rich
I finished tearing down motor last night and this is what I found.
I noticed a rusty stain next to a freeze plug, and thought it a good time to replace while accessible. I popped the plug and immediately found my problem. Sand.... and a lot of it. And yes, directly under the piston that had the meltdown. In fact the entire side of block was loaded with sand. The # 4 cylinder was almost buried in it. there was no circulation happening on that side of motor. If you recall, my #8 cylinder was showing sign of detonation as well. Apparently I must have done some good clammin with the outdrive the week before, during the night. I never knew how much sand i actually sucked in. Running in river up here, you sometimes get a lot closer to the bottom than you would like. I never ran it hard until the following week, when damage became apparent.
As for symptoms or lack of :
-Still had good water pressure ( yes I will still replace pump)
-Never showed hot on gage. Sending unit is next to thermostat and was still getting cold water flow
-The only thing I noticed was right side valve cover was getting hotter than other side.
So there it is in a nutshell. My bad..
I am still looking to get back in water with reasonable budget. I need pistons, heads, and will also replace valvetrain. I am trying to track down a set of 781's locally. If anyone has some hardware for sale, I will listen. Would like to stay with ovals. I would also appreciate some ideas regarding cam/piston/compression combo's that's been proven to work well. Thinking about staying with hydraulic flat tappet for budget reasons.I may upgrade rockers though. I have performer intake with 750 carb and EMI's to bolt up.
Thanks guys
Rich
#42
Registered
Joined: Dec 2006
Posts: 60
Likes: 0
My rat started knocking after coming off full throttle and this is what I found.
-Engine is GenIV 460 ci. Decked .010
-TRW L2465 pistons .226 dome
-Stock Peanut heads with some grind work, also milled .010 -Comp cam ,magnum #11-306-4 with .222 and .226 duration @.05, and .525 lift for both, and 110LSA
-Stock valve train except stronger springs
-Performer intake with 750edelbrock carb
-EMI exhaust
-Stock TBIV ignition
As I understand , these heads average about 119cc I estimate it has around 9.7:1 compression, without accounting for head mill. (maybe someone can help here)
As for quench, I estimate about .050 as is with stock gasket, but will verify this build.
Built with a budget at the time, and built for grunt, not top speed. Will still get me close to 65 in my 23fter at 5200rpm or so. Motor has maybe 150 hrs total. Surprisingly still had over 160 psi in that cylinder.Rings are still intact. Nothing went down below. Heads are still fine, but will verify. Runs on 93 octane.
Trying to get back in water and save some summer. What do you guys think caused this? I am no expert and could use some advice. Reversion? detonation? Other cylinders look fine, but this area seems washed on all of them.
As for rebuild, I'm thinking I may be ok down below. Will I be able to find this piston for replacement? I realize TRW has been absorbed by SpeedPro? Will a replacement piston be the same? I read somewhere about oilers being changed, etc. Not sure which way to proceed with this. I will remove that rod and check for straightness, and check bearing clearance. Anything else I should be doing? Thinking about checking all clearances while I am there. Not sure yet. Maybe re-bearing while open? Oil pressure is good. 65 at idle cold. I see some of my lifters have started to lose their crown. I will replace as well. Maybe time for a better cam? I wouldn't mind changing heads if price was right, or maybe open these up with bigger valves?
Always happy to get an extra mph or two. But have to stay somewhat reasonable with money.
Thanks for your insight.
Rich
-Engine is GenIV 460 ci. Decked .010
-TRW L2465 pistons .226 dome
-Stock Peanut heads with some grind work, also milled .010 -Comp cam ,magnum #11-306-4 with .222 and .226 duration @.05, and .525 lift for both, and 110LSA
-Stock valve train except stronger springs
-Performer intake with 750edelbrock carb
-EMI exhaust
-Stock TBIV ignition
As I understand , these heads average about 119cc I estimate it has around 9.7:1 compression, without accounting for head mill. (maybe someone can help here)
As for quench, I estimate about .050 as is with stock gasket, but will verify this build.
Built with a budget at the time, and built for grunt, not top speed. Will still get me close to 65 in my 23fter at 5200rpm or so. Motor has maybe 150 hrs total. Surprisingly still had over 160 psi in that cylinder.Rings are still intact. Nothing went down below. Heads are still fine, but will verify. Runs on 93 octane.
Trying to get back in water and save some summer. What do you guys think caused this? I am no expert and could use some advice. Reversion? detonation? Other cylinders look fine, but this area seems washed on all of them.
As for rebuild, I'm thinking I may be ok down below. Will I be able to find this piston for replacement? I realize TRW has been absorbed by SpeedPro? Will a replacement piston be the same? I read somewhere about oilers being changed, etc. Not sure which way to proceed with this. I will remove that rod and check for straightness, and check bearing clearance. Anything else I should be doing? Thinking about checking all clearances while I am there. Not sure yet. Maybe re-bearing while open? Oil pressure is good. 65 at idle cold. I see some of my lifters have started to lose their crown. I will replace as well. Maybe time for a better cam? I wouldn't mind changing heads if price was right, or maybe open these up with bigger valves?
Always happy to get an extra mph or two. But have to stay somewhat reasonable with money.
Thanks for your insight.
Rich
Curious about the picture in the 1st post. Did you take the picture upside down? If not, pistons are upside down. Just a thought!
#46
Rich,
As stated, the root cause of this failure is evident. The event originated as a localized hotspot, in the thinnest part of the crown. The detonation intensified further as the shallow, sharp edged area of the crown increased in temperature. The land area adjacent to the relief continued to lift until contact with the cylinder head was initiated, resulting in the loss of the ring land. The melted aluminum is clear in the photo. It is my understanding that a second piston was experiencing land deformation also but had not yet failed. The lack of heat discoloration outside of the area of the valve relief would indicate that the detonation was low-grade, localized near the sharp valve relief area of the piston crown. At this point the positive that can be taken away from this analysis would be how to move forward in the rebuilding the engine.
You stated your pistons are Speed Pro/TRW part number, L – 2465 – 030. They are a VMS – 75 high silicon piston, very similar in composition to a hypereutectic 4032 alloy, containing about 11% silicon. Hypereutectic pistons are relatively strong; however, in your instance it exemplifies one of the alloys main shortcomings. While the hypereutectic forgings display exceptional thermal stability, they lack the ductility and 2618 alloy. When detonation comes into play, the 2618 forging, a more malleable alternative, has a tendency toward plastic deformation. This can mitigate crack migration, potentially delaying/preventing eventual failure of the piston. A hypereutectic piston has a tendency to fracture immediately upon exceeding these limits. In the Marine environment, where prolonged high stress, high temperature, potential detonation, and sustained wide open throttle operation is routine, the hypereutectic piston is very unforgiving. While it is impossible to determine whether or not a 2618 alloy would've survived this particular event, you can make a case that it may have provided the necessary margin against catastrophic failure. This is a textbook example of why many engine builders specify the 2618 material exclusively for the marine environment.
Bob
As stated, the root cause of this failure is evident. The event originated as a localized hotspot, in the thinnest part of the crown. The detonation intensified further as the shallow, sharp edged area of the crown increased in temperature. The land area adjacent to the relief continued to lift until contact with the cylinder head was initiated, resulting in the loss of the ring land. The melted aluminum is clear in the photo. It is my understanding that a second piston was experiencing land deformation also but had not yet failed. The lack of heat discoloration outside of the area of the valve relief would indicate that the detonation was low-grade, localized near the sharp valve relief area of the piston crown. At this point the positive that can be taken away from this analysis would be how to move forward in the rebuilding the engine.
You stated your pistons are Speed Pro/TRW part number, L – 2465 – 030. They are a VMS – 75 high silicon piston, very similar in composition to a hypereutectic 4032 alloy, containing about 11% silicon. Hypereutectic pistons are relatively strong; however, in your instance it exemplifies one of the alloys main shortcomings. While the hypereutectic forgings display exceptional thermal stability, they lack the ductility and 2618 alloy. When detonation comes into play, the 2618 forging, a more malleable alternative, has a tendency toward plastic deformation. This can mitigate crack migration, potentially delaying/preventing eventual failure of the piston. A hypereutectic piston has a tendency to fracture immediately upon exceeding these limits. In the Marine environment, where prolonged high stress, high temperature, potential detonation, and sustained wide open throttle operation is routine, the hypereutectic piston is very unforgiving. While it is impossible to determine whether or not a 2618 alloy would've survived this particular event, you can make a case that it may have provided the necessary margin against catastrophic failure. This is a textbook example of why many engine builders specify the 2618 material exclusively for the marine environment.
Bob
#47
Registered
Joined: Jun 2011
Posts: 197
Likes: 2
Well I am glad there is sombody else on the same page as me I mentioned the timming earlier and there was no response.
#48
Updates to follow. Thanks,
Rich
#50
Was pretty hard trying to keep my boat from turning into another back yard project with all the non boating distractions that popped up this year, but here we are...
Motor is now in and alignment is done. Should hopefully hear it come to life in a day or so... Wish me luck..
Also attached a pic of root cause of last failure. Discerning eyes will find the culprit. Mea Culpa.
Motor is now in and alignment is done. Should hopefully hear it come to life in a day or so... Wish me luck..
Also attached a pic of root cause of last failure. Discerning eyes will find the culprit. Mea Culpa.


