What type EGT probes
#11
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Joined: Aug 2011
Posts: 2,733
Likes: 8
From: bel air, md
Thanks guys for the info but I guess what I am asking what type probes for EGT and 02 and is there a management systems or gauges to just read the probes I am 1050 carb do not want it to make adjustments I will be pulling all over. I live in Tn pull to Phoenix 2 times a year. I would like this for tunning.
Thanks AJ
Thanks AJ
#12
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Joined: Jun 2009
Posts: 9,981
Likes: 6,477
From: Chicago
Very Loose rotor in the distributor advanced the timing to who knows what
http://33outlaw.zenfolio.com/img/s1/v5/o548260849/c1/p1564372673-220.mp4





http://33outlaw.zenfolio.com/img/s1/v5/o548260849/c1/p1564372673-220.mp4





Last edited by ICDEDPPL; 11-30-2015 at 11:43 PM.
#16
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Joined: Jul 2004
Posts: 11,332
Likes: 73
From: chicago
Dan caught alot of slack from the video he had with thr gopro mounted in the bilge, showing smoke coming out of the breathers. At the time of the video, he also had a moisture issue with his oil, and had a significant amount of milkshake going on. I believe what was coming out of the valve covers in that video, was actually steam, and not oil smoke.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
#17
Registered
Joined: Aug 2011
Posts: 2,733
Likes: 8
From: bel air, md
Dan caught alot of slack from the video he had with thr gopro mounted in the bilge, showing smoke coming out of the breathers. At the time of the video, he also had a moisture issue with his oil, and had a significant amount of milkshake going on. I believe what was coming out of the valve covers in that video, was actually steam, and not oil smoke.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
#18
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Joined: Jul 2004
Posts: 11,332
Likes: 73
From: chicago
Nah. Weird thing was the concave lock washers, literally rusted and disintegrated. Other engines washers look brand new. Both replaced at same time .
Last edited by MILD THUNDER; 12-01-2015 at 10:03 AM.
#19
Registered
Joined: Jul 2012
Posts: 1,248
Likes: 3
From: indianapolis
Dan caught alot of slack from the video he had with thr gopro mounted in the bilge, showing smoke coming out of the breathers. At the time of the video, he also had a moisture issue with his oil, and had a significant amount of milkshake going on. I believe what was coming out of the valve covers in that video, was actually steam, and not oil smoke.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
#20
Dan caught alot of slack from the video he had with thr gopro mounted in the bilge, showing smoke coming out of the breathers. At the time of the video, he also had a moisture issue with his oil, and had a significant amount of milkshake going on. I believe what was coming out of the valve covers in that video, was actually steam, and not oil smoke.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
Irregardless, those engines consumed a bunch of oil, and were due for rebuilds.
Im no expert on failure analysis, his rotor screws had came loose from failed lock washers on one engine. The rotor screws were so loose, it allowed the rotor locating tab, to even become disengaged from the distributor.
My initial thoughts, were the timing became excessively retarded while he was running wfo for a long stretch during his last boating outing, piston got extremely hot, and began scuffing the bore, and tuliping an exhaust valve.
The other engine, which had the same tune, had no damage, still showed good on the compression test and fair on the leakdown. Engine with rotor coming loose, had damaged piston, and tuliped exhaust valve.
Thats just my theory, and it could be way off.
Last edited by Knot 4 Me; 12-01-2015 at 10:02 AM.


