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Im not sure what chargers your running?? My M-3 will sit around the 2 PSI mark at about 3100 RPM, to me the boost should be coming in sooner then 4000 RPM (granted I dont know what pulleys/blowers your actually running) Whats the back of the boat look like? Soot?? What do your plugs look like?? Have you watch timing on a timing light to see how it reacts?
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It has to be an ignition problem or a fuel problem, if the motor is sound inside.
Didn't read all posts, but did you do a compression test hot.. I had a problem with detonation and it broke the ring lands on the piston before. It wouldnt show up on a cold comp test. |
Originally Posted by resurrected
(Post 4796524)
The fuel you are using is crap and the knock senors pulling them back? Just throwing out stuff because I don't think there is much left
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Originally Posted by Ontariocheckmate
(Post 4796529)
Im not sure what chargers your running?? My M-3 will sit around the 2 PSI mark at about 3100 RPM, to me the boost should be coming in sooner then 4000 RPM (granted I dont know what pulleys/blowers your actually running) Whats the back of the boat look like? Soot?? What do your plugs look like?? Have you watch timing on a timing light to see how it reacts?
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Originally Posted by bossbrakes
(Post 4796538)
It has to be an ignition problem or a fuel problem, if the motor is sound inside.
Didn't read all posts, but did you do a compression test hot.. I had a problem with detonation and it broke the ring lands on the piston before. It wouldnt show up on a cold comp test. |
Hmmm definitely very confusing for sure... the only time Ive seen a similar issue with my boat was when I was trying different props this year, Just simply wasnt putting out the boost or pulling the proper RPM... swap back the props everything was good. You havnt changed your props though at all correct?
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Originally Posted by Ontariocheckmate
(Post 4796627)
Hmmm definitely very confusing for sure... the only time Ive seen a similar issue with my boat was when I was trying different props this year, Just simply wasnt putting out the boost or pulling the proper RPM... swap back the props everything was good. You havnt changed your props though at all correct?
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How about full throttle travel at the TB?
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Originally Posted by resurrected
(Post 4796640)
How about full throttle travel at the TB?
Thanks everyone for all the suggestions - I've gotta get this figured out! |
I can't wait to hear the solution! This is a head scratch-er for sure. Keep digging, the season is too short to be head down @$$ up in the bilge all summer!
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friend of mine works @ Pro charger here in KC, have you called them ?
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Definately is a dam interesting one thats for sure! I also cant wait to hear what ya find! Another thing you could try is dropping the pulley size down one, this will bring your boost in at a lower RPM, I downsized mine by 1 size recently because it wasnt building full boost at WOT. I know your having a different problem but would be interesting to see what procharger says about it.
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Originally Posted by F-2 Speedy
(Post 4796653)
friend of mine works @ Pro charger here in KC, have you called them ?
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Ive not read this complete thread but could it be a timing issue, are your ecm's locked or can you get into them and look at the timing and fuel tables ? have you verified 8* of timing in base timing mode and full advance ?
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on the bottom of the hull,,is there anything in the water path to the motors prop that spins up?are there drive showers?is the trim indicator true to the drives position?
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This is a long shot, but was anything done to boat that would restrict air coming into engine compartment? Reason I ask is on mine I found a couple of the bilge air inlets taped over inside the bilge when I removed the vents for waxing. Maybe try cracking open hatch an inch or so while running?
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These are 540's with M1 Prochargers? I'm shocked that they make any boost.
Out of curiosity, what did they dyno? I can't wait to hear the fix. I leak tested an engine a bit ago and it leaked down good. When the heads were removed it was missing part of the pistons I believe on the exhaust side. Engine was down a little on power, but nothing that would have said tops of pistons melted. |
L was going to say to check the air inlet , do you have an exhaust leak in the engine compartment that is polluting the intake air?
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Originally Posted by F-2 Speedy
(Post 4796681)
Ive not read this complete thread but could it be a timing issue, are your ecm's locked or can you get into them and look at the timing and fuel tables ? have you verified 8* of timing in base timing mode and full advance ?
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Originally Posted by zz28zz
(Post 4796765)
This is a long shot, but was anything done to boat that would restrict air coming into engine compartment? Reason I ask is on mine I found a couple of the bilge air inlets taped over inside the bilge when I removed the vents for waxing. Maybe try cracking open hatch an inch or so while running?
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Originally Posted by Rookie
(Post 4796865)
These are 540's with M1 Prochargers? I'm shocked that they make any boost.
Out of curiosity, what did they dyno? I can't wait to hear the fix. I leak tested an engine a bit ago and it leaked down good. When the heads were removed it was missing part of the pistons I believe on the exhaust side. Engine was down a little on power, but nothing that would have said tops of pistons melted. |
So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?
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Originally Posted by splashandburn
(Post 4797155)
hy wouldn't you think they made any boost? I've run this set up for years and always pushed out 5 psi at the plenom. They actually dynoed @ 930 @ 5500. I know Procharger doesn't rate them that high but never had an issue until now and all we did was a valve job.
Have you borescoped a few cylinders? Thanks |
Originally Posted by splashandburn
(Post 4797156)
So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?
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https://cimg8.ibsrv.net/gimg/www.off...a6150b5b6a.jpg
Pulled tubing off just before intake and there's definitely positive airflow there. |
Have you pulled the pulleys off each charger and inspected the keyway? Long shot but maybe slipping under load/high rpm if keyway is wore/key broke?? Very odd and confusing problem for dam sure, Almost at a loss and makes zero sense as to why it would be pulling a vacuum at high rpm when theres positive airflow at idle
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Originally Posted by splashandburn
(Post 4797156)
So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?
https://cimg5.ibsrv.net/gimg/www.off...6544b27cf3.gif |
If it we’re mine, I’d swap the chargers, inter coolers and ducting between the 2
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Originally Posted by JaayTeee
(Post 4797376)
If it we’re mine, I’d swap the chargers, inter coolers and ducting between the 2
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5+" of vac at WOT?! Sounds like blower is getting in the way.
Could there be slippage at crank pulley? |
Originally Posted by zz28zz
(Post 4797539)
5+" of vac at WOT?! Sounds like blower is getting in the way.
Could there be slippage at crank pulley? |
Originally Posted by splashandburn
(Post 4797579)
checked the keyways there too and everything checks out. We're trying smaller blower pulleys next with the thought that the motor is eating up all the boost the blowers are producing. The fact that the boost went totally away and went to a vacuum as we increased engine rpm kinda points that way. Hoping to increase the boost at the same engine rpm with smaller pulleys is the answer. Fingers crossed!
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Originally Posted by splashandburn
(Post 4797579)
checked the keyways there too and everything checks out. We're trying smaller blower pulleys next with the thought that the motor is eating up all the boost the blowers are producing. The fact that the boost went totally away and went to a vacuum as we increased engine rpm kinda points that way. Hoping to increase the boost at the same engine rpm with smaller pulleys is the answer. Fingers crossed!
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Could the blower belt/s be contaminated with oil, fuel, p/s fluid, cleaning/detailing products, etc?
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Originally Posted by zz28zz
(Post 4797721)
Could the blower belt/s be contaminated with oil, fuel, p/s fluid, cleaning/detailing products, etc?
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Any update on this?
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Crazy question, is the Drive pulley actually turning the impeller on the SC in question? or turning under load ( implying possible internal damage of the SC).
Thinking out loud, if it's not compressing, it's working as an air block as the engine is after more than it can draw through the system = no boost and drop in RPM's |
So here's an update but still no fix. Decided to pull one of the motors and run it back on the dyno. Motor ran fine - 950 hp and 1000 ft lbs of torque. Put the motor back in the boat and its doing exactly the same thing - 4000 rpm max and showing no boost. This is really frustrating. Boat always ran great.
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In what condition was the engine on the dyno, full marine trim?
What is different between dyno and in the boat, Fuel system? Ignition system? Exhaust? Cooling water? The problem lies in the differences somewhere? Ryan |
Originally Posted by Ballistic Beak
(Post 4799874)
In what condition was the engine on the dyno, full marine trim?
What is different between dyno and in the boat, Fuel system? Ignition system? Exhaust? Cooling water? The problem lies in the differences somewhere? Ryan |
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