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splashandburn 07-12-2021 04:21 PM


Originally Posted by Rookie (Post 4796865)
These are 540's with M1 Prochargers? I'm shocked that they make any boost.
Out of curiosity, what did they dyno?
I can't wait to hear the fix.
I leak tested an engine a bit ago and it leaked down good. When the heads were removed it was missing part of the pistons I believe on the exhaust side. Engine was down a little on power, but nothing that would have said tops of pistons melted.

Yes 540's with M1-SC chargers. Why wouldn't you think they made any boost? I've run this set up for years and always pushed out 5 psi at the plenom. They actually dynoed @ 930 @ 5500. I know Procharger doesn't rate them that high but never had an issue until now and all we did was a valve job.

splashandburn 07-12-2021 04:24 PM

So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?

Rookie 07-12-2021 09:59 PM


Originally Posted by splashandburn (Post 4797155)
hy wouldn't you think they made any boost? I've run this set up for years and always pushed out 5 psi at the plenom. They actually dynoed @ 930 @ 5500. I know Procharger doesn't rate them that high but never had an issue until now and all we did was a valve job.

I guess not. I thought they were a 700HP supercharger. Good to know, that opens up options.
Have you borescoped a few cylinders?
Thanks

Ontariocheckmate 07-13-2021 05:11 AM


Originally Posted by splashandburn (Post 4797156)
So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?

To me the only way thats possible at all (provided that the boost/vacuum gauges are both accurate) Is that theres something internally wrong with either charger, or theres a boost leak in both systems. If your building the engine RPM which your are you should most definitely be building boost. The weirdest thing about your problem is your having the issue with both motors. What did procharger say when you contacted them? How does your setup work on yours? As in airflow... charger, intercooler then into the plenum? Have you tried pulling one of the connections and verified positive airflow?

splashandburn 07-13-2021 10:44 AM

https://cimg8.ibsrv.net/gimg/www.off...a6150b5b6a.jpg

Pulled tubing off just before intake and there's definitely positive airflow there.

Ontariocheckmate 07-13-2021 10:55 AM

Have you pulled the pulleys off each charger and inspected the keyway? Long shot but maybe slipping under load/high rpm if keyway is wore/key broke?? Very odd and confusing problem for dam sure, Almost at a loss and makes zero sense as to why it would be pulling a vacuum at high rpm when theres positive airflow at idle

SB 07-13-2021 11:03 AM


Originally Posted by splashandburn (Post 4797156)
So I ran smaller props over the weekend to get more rpm and spin the Prochargers faster. Got it up to around 4800 rpm and the boost gauges actually show about 5+ inches of vacuum! How's that even possible?

Damn !

https://cimg5.ibsrv.net/gimg/www.off...6544b27cf3.gif

JaayTeee 07-13-2021 06:53 PM

If it we’re mine, I’d swap the chargers, inter coolers and ducting between the 2

cheech 07-13-2021 10:03 PM


Originally Posted by JaayTeee (Post 4797376)
If it we’re mine, I’d swap the chargers, inter coolers and ducting between the 2

See post 37!

zz28zz 07-14-2021 03:03 PM

5+" of vac at WOT?! Sounds like blower is getting in the way.

Could there be slippage at crank pulley?


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