Go Back  Offshoreonly.com > Owners Forum > Formula
My new project - 86 - 272 LS >

My new project - 86 - 272 LS

Notices
Formula

My new project - 86 - 272 LS

Thread Tools
 
Old 07-25-2012, 08:00 AM
  #101  
Gold Member
Gold Member
 
Join Date: Jan 2011
Location: Syracuse, NY
Posts: 1,097
Likes: 0
Received 0 Likes on 0 Posts
Default

befu if I can offer advice... Went through this t-bolt IV crap earlier this year. Pull them off, drop HEI dizzy's on and rewire the tack and shift interrupt. It's $400 more now, and 10yrs of reliability. No trouble shooting and checking a million things.
machloosy is offline  
Old 07-25-2012, 11:06 AM
  #102  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default

Originally Posted by machloosy
befu if I can offer advice... Went through this t-bolt IV crap earlier this year. Pull them off, drop HEI dizzy's on and rewire the tack and shift interrupt. It's $400 more now, and 10yrs of reliability. No trouble shooting and checking a million things.
Yeah, had a mechanic suggest the HEI route also. I think we got it to work, had the timing off. Must not of had a good ground when we tried to see a spark.

Should get a chance to see some results tomorrow.

Sprink, I do not know and no!

I pulled it through the parking lot out to the main road. Went 130 yards to the gas station and then back. Not sure if I hit 10 MPH! No plate, no lights, no brakes..... We are out in the country, so no problem. We will get the brakes working with the new 7 pin connector installed later this week or next week.

Time to make the wife cringe and go order more stuff...

Brian
befu is offline  
Old 07-25-2012, 06:09 PM
  #103  
Charter Member #232
Charter Member
 
Audiofn's Avatar
 
Join Date: Oct 2000
Location: Carlisle, MA USA
Posts: 18,422
Received 6 Likes on 4 Posts
Default

With those older ignitions they often times had two wires go to the coil. One for when the boat was running that was at a lower voltage, Then one that came from the starter if memory serves that was a 12 volt while cranking to get a real hot spark to make it fire due to the lowered voltage while cranking. You can test with a jumper wire if you need to.
__________________
Put your best foot forward!
Audiofn is offline  
Old 07-26-2012, 02:29 PM
  #104  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default

Got the starboard motor running, sounds good! Runs so well it wouldn't shut off! Had to turn out the idle screw to drop it low enough to stall it. So, something is not killing voltage to the ignition, will have to look into that one.

Port motor not getting fuel into the carb, so we are pulling it back off, I think I did something wrong with the float. First time, the carb flooded and leaked fuel out of it like the needle didn't close. Now it doesn't fill and is empty, odd.

Also had an issue with the fuel pump not priming where it is, so I think I am going to move it down to the bulk head right behind the fuel tank. Still have some issues to work on, but making progress.

Brian
befu is offline  
Old 08-08-2012, 04:43 PM
  #105  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default updates

Lots of stuff done.

Spent some time and got the drive pucks all dialed in. Both trim to the same height and stop. Both drive position gauges read pretty dang good. Put a layer of electrical tape over the puck spline before putting them back on the drive and that helped a lot. Before there was too much slop and the drive would have to move too far before the gauge moved. Now I can adjust the drives and they are within a half inch of each other. Not bad for the old 26 years old stuff!

Ran the Starboard motor again today and ran great. Had to tighten a couple of hoses, but it started well, good throttle response, put the new secondary jets in it also. Oil pressure is good, temp never came up but the water coming out of the thermostat housing got hot and the exhaust manifolds remained cold. Also running it on well water that is coming out of ground cold, so not surprised.

shifted the drive into forward and reverse, sounded fine and worked great.

Motor still not shutting off. Ignition kills voltage to coil, so I am back feeding from alternator. will post more on this later with pics.

Port motor is still no go. Took three tries, but got the float adjusted in the carb and it works great now. Just no spark at all. voltage on the coil, so we will have to start going through it. The motor did start and run last fall, so not sure what it is. Thought it was wired up correctly, we will have to see. Oh, no spark at the input to the distributor, so seems like coil or ignition module is stopping it due to wiring issue.

Also started gluing down the new carpet in the cabin section, makes a big improvement in the way it looks! also started to fix the seat side that my big a$$ broke when I sat down, will document that in a single post when done to show how I did it.

A couple of pics of it on the reworked trailer outside for the second time this year!

Brian
actually running


In the sun! man I need to remove that bottom paint!


Back end view
befu is offline  
Old 08-09-2012, 08:12 AM
  #106  
Gold Member
Gold Member
 
Join Date: Jan 2011
Location: Syracuse, NY
Posts: 1,097
Likes: 0
Received 0 Likes on 0 Posts
Default

Can't wait to get my hands on a 272 next year. Yours looks real sharp Brian. Keep up the work!
machloosy is offline  
Old 08-16-2012, 08:33 PM
  #107  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default

Thanks machloosy, lots of good deals out there. Don't buy one like I did, ton of work into this one.

OK, pic of the transom - got the props installed. And no crap about the props OK, they are the 4 blade - 21 pitch for local lakes and tubing. I have a set of 23 SS ones for speed. All I need now on the transom is the drain plug.

Finished up the floor and bench carpet for the cabin area. Not great, but first time I tried this. Porti potti fits great and will now be usable for all my kids. I am going to recover the old bench cushions and reuse the foam. Where the old cooler and cupboards were I am going to build in some storage areas for towable toys, cooler, life jacket and such so it is not flying around. Front bulkheads will also be carpeted once I figure out how I am doing the front of the boat.

Maybe tomorrow, definately Monday I plan on trying the port motor out and see how it does. maybe spash it next week....

Brian




befu is offline  
Old 08-21-2012, 11:10 AM
  #108  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default

I had mentioned earlier that I would do a complete post on how I fixed one of the sides on my seats. On these, the main seat is all attached to a very solid piece of fiberglass in the overall shape of a L. The two sides then bolt to this with 4 bolts each. On mine, the wood had gotten wet so the retaining nuts had rusted away and the wood was soft allowing the remains to just spin or pull out - so I rebuilt them with new attachment nuts. Well, the first time I sat in one, the side of it popped right off, appears the repair was not as good as I hoped.

First thing I did was to remove all the staples from the back fo the side and remove the vinyl skin. This went pretty straight forward. What I found was a piece of molded expanding foam with a 1/2" piece of plywood on the inside of it. The whole thing was covered by that 1/8" foam and then the skin was put over it. Well, the bottom 1/2 of the plywood was so bad, the new attachment nuts just pulled out bigger pieces of wood. So I started digging and I removed all of the bad plywood down to the foam piece. I marked where the nuts were and ended up putting weld studs in three of them since the wood was 100% gone.

After the weld studs were in place and everything was cleaned up, I really saturated the remaining wood working resin into it. I wanted to following repair to really bite into the old good wood. I added a few layers of fiberglass over the foam and worked it over the top of the old wood. Once that was cured, I made up a thickened slurry of resin and used that to squish down a piece of 1/4" plywood to the first layers of glass.

Continued.....


The main part of the seat with the side panel removed


The seat filler with the bad wood removed. Plus you can use it in the flower bed as mulch!


Glass over the foam with new attachment hardware in there


1/4" ply set in place with a slurry mixture of thickened resin
befu is offline  
Old 08-21-2012, 11:23 AM
  #109  
Registered
Thread Starter
iTrader: (2)
 
Join Date: Jan 2011
Location: NE Indiana
Posts: 956
Likes: 0
Received 2 Likes on 2 Posts
Default seat repair continued

Once the filler piece of plywood was in, I used some more slurry to fill in around the edges. Then I added a few more layers of glass over the seam tapered down to one layer over the good wood. With that done, I let it cure again. Used some spray adhesive to hold down the piece of thin foam that I had pealed up, trimmed up any glass fibers sticking out and stuffed it back into the vinyl sleeve. It fits!

I pulled the vinyl tight and started stapling it in and this is where I discovered my mistake. The thing is so strong and solid, I can not staple the vinyl back on except for a few places. I even tried a brad nailer - it worked some but where the glass was too solid it just bent the brad. So I predrilled holes and used some small stainless screws to secure the vinyl skin.

It turned out really strong! I guess I didn't need to do that much work, but it is one thing I do not need to worry about breaking. I sat in the othe seat and bumped it around, appears solid so it looks like I get away with only rebuilding one of the sides.

And the project marches on.......

Plywood filler glassed over


stuffed back into the skin with foam glued down


Ready for install
befu is offline  
Old 08-21-2012, 11:29 AM
  #110  
Registered
VIP Member
 
Join Date: Aug 2012
Location: Alexandria Bay, NY
Posts: 93
Likes: 0
Received 0 Likes on 0 Posts
Default

Befu very nice work. Wish I had your talent for the upholstery work, I am a engine guy and I can do the wiring but I suck at upholstery work. I cannot wait to see the final pictures. I might have missed it but what are you running for power?
EMSDiver is offline  


Contact Us - Archive - Advertising - Cookie Policy - Privacy Statement - Terms of Service

Copyright © 2024 MH Sub I, LLC dba Internet Brands. All rights reserved. Use of this site indicates your consent to the Terms of Use.