12:1 compression ratio
#21
big diffrence in a boat vs a car.the boat motor runs under 100% load all the time,unlike a car.i say use the highest octane you can find.better to be safe than sorry.after all,gas is the cheapest thing about boating.
#22
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From: Between A Womans Leggs in IL
timing is 32, specs of the pistones are the following:
Bore (in) 4.530 in.
Bore (mm) 115.062mm
Piston Style Dome, with single valve relief
Piston Material Forged aluminum
Compression Distance (in) 1.395 in.
Piston Head Volume (cc) -21.00cc
Wrist Pin Style Press-fit or floating
Pin Diameter (in) 0.990 in.
would lowering the timming help?
Bore (in) 4.530 in.
Bore (mm) 115.062mm
Piston Style Dome, with single valve relief
Piston Material Forged aluminum
Compression Distance (in) 1.395 in.
Piston Head Volume (cc) -21.00cc
Wrist Pin Style Press-fit or floating
Pin Diameter (in) 0.990 in.
would lowering the timming help?
like bob said you could radius the piston crown to relieve some compression, also get rid of the sharp points on the piston's, this will help with detonation. Take Bob's advise,he wont steer you wrong..if you use a thicker mls head gasket, i wouldn't go no more the .051 thick make sure you use head studs.. i run 10.2-1 in my little boat,355sbc on 93 fuel for 10 yrs,never no issues.. keep it cool and it should be fine..
Last edited by FIXX; 04-29-2010 at 09:33 AM.
#23
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From: Vancouver BC
What heads are you using? Are you sure you're 12:1? There are many ways to crutch your engine and make it run but none of them are right. Especially given the fact that you're building a second motor. The right thing to do and cheapest in the long run is to pull your motor apart and have the domes cut down. They are mos likely a solid dome and any competent machine shop will be able to mill the domes easily.
Also mrfixx the increased cylinder pressure from a SC is different then a high static comp ratio and running a thicker gasket to compensate on a NA motor is probably worse then running proper quench.. My .02
Also mrfixx the increased cylinder pressure from a SC is different then a high static comp ratio and running a thicker gasket to compensate on a NA motor is probably worse then running proper quench.. My .02
Last edited by HaxbySpeed; 04-29-2010 at 10:41 AM.
#24
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From: Between A Womans Leggs in IL
Also mrfixx the increased cylinder pressure from a SC is different then a high static comp ratio and running a thicker gasket to compensate on a NA motor is probably worse then running proper quench.. My 02..
that would depend on his deck height,, cheers
that would depend on his deck height,, cheers
#27
Cafe,
I would recommend against retarding the timing to prevent detonation as it will elevate your EGT figure significantly. Your actual compression ration is not 12:1. It ranges anywhere from 10.350:1 w/ 121 cc combustion chamber to 10.783:1 w/ 116 cc combustion chamber. These are easily managed numbers with 95 (RON+MON)/2 fuel.
Bob
I would recommend against retarding the timing to prevent detonation as it will elevate your EGT figure significantly. Your actual compression ration is not 12:1. It ranges anywhere from 10.350:1 w/ 121 cc combustion chamber to 10.783:1 w/ 116 cc combustion chamber. These are easily managed numbers with 95 (RON+MON)/2 fuel.
Bob
#30
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From: Between A Womans Leggs in IL



