Erratic Vaccuum readings
#21
Registered
Joined: Dec 2010
Posts: 108
Likes: 0
From: Arizona
If you are certain you have eliminated leaking exhausts, then it sounds like a headgasket issue. unless you left water in the motor and it froze over the winter possibly cracking the heads and or the cylinder bores.
It seems really odd that just the front two are having issues.
could you post a video link of it happening from smooth startup to when it starts missing? You tube or something...
It seems really odd that just the front two are having issues.
could you post a video link of it happening from smooth startup to when it starts missing? You tube or something...
#22
Thread Starter
Registered

Joined: Nov 2012
Posts: 141
Likes: 39
From: H.B. CA
If you are certain you have eliminated leaking exhausts, then it sounds like a headgasket issue. unless you left water in the motor and it froze over the winter possibly cracking the heads and or the cylinder bores.
It seems really odd that just the front two are having issues.
could you post a video link of it happening from smooth startup to when it starts missing? You tube or something...
It seems really odd that just the front two are having issues.
could you post a video link of it happening from smooth startup to when it starts missing? You tube or something...
#25
Registered
Joined: Sep 2010
Posts: 98
Likes: 0
From: Fort Walton Bch. FL.
#27
Registered
Joined: Dec 2010
Posts: 108
Likes: 0
From: Arizona
I dont know does it get be freezing, where you are at in cali? Water turning into ice will crack metal easier then you snapping a toothpick.
If you think its a water issue, just remove the water from the equation as I have recommended prior. You wont overheat it idleing for 3 mins.
If you think its a water issue, just remove the water from the equation as I have recommended prior. You wont overheat it idleing for 3 mins.
#29
Thread Starter
Registered

Joined: Nov 2012
Posts: 141
Likes: 39
From: H.B. CA
Well I figured it out!! STUCK VALVE. Did a leak down test and found air coming out of the #2 exhaust port. The reversion was from the open valve that was sucking water and shut down my spark plug. So I pulled the head sprayed WD40 on it and it went right back in but seem a little tight. No salt water reversion it's from the hose.
Is this happening because it hasn't been started for four months or should I look for something else?
What should I do to fix this?
Is this happening because it hasn't been started for four months or should I look for something else?
What should I do to fix this?



