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Mighta made an oopsie. Name that Knock!

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Old 08-11-2022 | 03:57 PM
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You suspected carbon build-up initially thus the steam cleaning. Maybe the water vapor caused localized cooling of the valve guide causing it to shrink just a hair making the carboned-up exh valve stick open??

On the brighter side, looks like you'll have a chance to address #7 while you have the head off.
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Old 08-11-2022 | 03:58 PM
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Originally Posted by DrFeelgood
There is a small amount of rust in the exhaust ports of cyls 5 and 7 in that header. Not a lot, but there is some. There also was a little bit of water in the bottom of the V-band clamp at the header-tailpipe junction.
A pressure test is in order my friend.
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Old 08-11-2022 | 04:13 PM
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On the bright side, you may have inadvertently discovered a huge problem that left unchecked could have caused a catastrophic destruction of your engine. Leaky headers have destroyed many thus the design change.
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Old 08-11-2022 | 04:27 PM
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you got lucky that piece of guide plate didn't go down under............
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Old 08-11-2022 | 06:09 PM
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If you had enough cylinder pressure your piston rod can look like your pushrod.
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Old 08-11-2022 | 07:22 PM
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If I pull cylinder head this weekend, and the tops of the pistons look fine, what's the chances that this is purely a top end problem and the bottom end is fine?
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Old 08-11-2022 | 07:40 PM
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Let me get this right... You poured water down the PCV hose? You did not mist into the throttle body?
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Old 08-12-2022 | 04:01 AM
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Originally Posted by Rookie
Let me get this right... You poured water down the PCV hose? You did not mist into the throttle body?
"poured" is a strong word.

"Trickled" into the hose would be a more accurate word.

I've done this before on other engines (including the starboard one 5 minutes earlier) with no ill effects.

Pending final analysis of what went wrong, I reserve the right to re-evaluate my choices

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Old 08-12-2022 | 07:29 AM
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Originally Posted by DrFeelgood
"poured" is a strong word.

"Trickled" into the hose would be a more accurate word.

I've done this before on other engines (including the starboard one 5 minutes earlier) with no ill effects.

Pending final analysis of what went wrong, I reserve the right to re-evaluate my choices
You and Eddie sure have bad luck when it comes to boat motors.
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Old 08-12-2022 | 07:48 AM
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Originally Posted by Wildman_grafix
You and Eddie sure have bad luck when it comes to boat motors.
Yeah, I've noticed that. Though, I can't really get too upset, I bought this thing with no real knowledge of how/when/if these motors had any real work done to them in the last 20 years. Best I can tell, the motors were redone in 2003-2004 with no evidence of being opened up since, and somewhere around 450-500 hours on them since then.

Even if I had the leakdowns done prior to purchase I don't know that it would have been bad enough to make me not buy it.

When I bought the Cigarette, I bought it with the knowledge that the motors were recently built, and got a false sense of security about the likely reliability of what turned out to be very sub-par builds.



Last edited by DrFeelgood; 08-12-2022 at 07:53 AM.
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